Accident McDonnell Douglas DC-8-62F N990CF,
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ASN Wikibase Occurrence # 323520
 

Date:Thursday 27 April 2000
Time:21:30
Type:Silhouette image of generic DC86 model; specific model in this crash may look slightly different    
McDonnell Douglas DC-8-62F
Owner/operator:Emery Worldwide
Registration: N990CF
MSN: 46068/463
Year of manufacture:1969
Total airframe hrs:51844 hours
Fatalities:Fatalities: 0 / Occupants: 5
Aircraft damage: Substantial, repaired
Category:Accident
Location:Denver, CO -   United States of America
Phase: En route
Nature:Cargo
Departure airport:Seattle/Tacoma International Airport, WA (SEA/KSEA)
Destination airport:Dayton-James Cox Dayton International Airport, OH (DAY/KDAY)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
A Douglas DC-8-62F, N990CF, was substantially damaged when the number two engine cowling departed the airplane near Denver, Colorado. The three flight crew members and two passengers were not injured. Visual meteorological conditions prevailed for the night cross-country flight, which originated from Seattle, Washington, 2 hours 48 minutes before the accident. An IFR flight plan had been filed for the cargo flight that was en route to Dayton, Ohio.

The captain said that they were in cruise flight at 37,000 feet mean sea level (msl). He said that they heard a loud bang and the airplane shook, and they immediately began to lose cabin pressurization. The engine instruments went dead on number two- engine, and they pulled the number two emergency "T" handle. He said that they donned their oxygen masks, began descending, and diverted to Denver. Their landing was uneventful.
Post landing examination of the number two-engine nacelle revealed that the inboard and outboard main engine cowlings had separated from the aircraft. An 18x6 inch hole was found half way up the fuselage (pressure bulkhead), just aft of the left wing; the left horizontal stabiliser was also damaged. Further examination of the engine revealed that the 4 inch-diameter high pressure bleed air duct had separated from the high-pressure relief valve, and the connecting clamp was missing. The clamp was never located.
The wire bundle, which transmitted the number two engine monitoring data to the cockpit, was found cut. There was no evidence of engine fire, or fire in the nacelle cavity.

According to the operator: "when the clamp assembly failed, high pressure bleed air from the 4 inch diameter duct dumped into the area inside of the engine cowlings. The sudden over-pressurization probably expanded the main engine cowlings into the air stream, leading to the loss of the cowlings. The amount of airflow from the high pressurization bleed air duct far exceeds the air discharge capacities of the cowling blow out panels."

PROBABLE CAUSE: "The failure of the clamp that secured the high-pressure bleed air duct to the high-pressure relief valve. Factors were the resulting excessive pressurization of the engine nacelle, and the subsequent separation of the engine cowling."

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN00FA078
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB

Revision history:

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