ASN Wikibase Occurrence # 323242
Date: | Saturday 25 August 2001 |
Time: | 01:11 |
Type: | Boeing 737-3G7 |
Owner/operator: | America West Airlines |
Registration: | N306AW |
MSN: | 24633/1809 |
Year of manufacture: | 1990 |
Total airframe hrs: | 37875 hours |
Fatalities: | Fatalities: 0 / Occupants: 59 |
Aircraft damage: | Substantial, repaired |
Category: | Accident |
Location: | Baltimore/Washington International Airport, MD (BWI) -
United States of America
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Phase: | Landing |
Nature: | Passenger - Scheduled |
Departure airport: | Phoenix-Sky Harbor International Airport, AZ (PHX/KPHX) |
Destination airport: | Kansas City International Airport, MO (MCI/KMCI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A Boeing 737-3G7, N306AW, operated by America West Airlines, sustained foreign object damage (FOD) to both engines during landing when it veered off the left side of runway 27 (9,500 feet by 150 feet, wet grooved asphalt) at the Kansas City International Airport (MCI), Missouri.
The transport airplane sustained substantial damage during landing when it veered off the left side of runway 27 at 0111 CST and both engines sustained foreign object damage (FOD).
Level 4 and 5 thunderstorms were in the vicinity of the airport at the time of the accident. The ASOS rain gauge on the airport indicated 0.42 inches of rain fell between 01:00 and 01:11. The wind was from the northwest at less than 10 knots, and no significant low-level windshear was present at the time of the accident. The first officer was the flying pilot.
The Flight Data Recorder data indicated the airplane was on a stabilized instrument approach with the autopilot engaged until about 200 feet above ground level (agl), when the autopilot was disconnected and the airplane was flown manually. After the autopilot disconnect, the airplane began drifting left and above glide slope. The airplane crossed the runway threshold at about 57 feet agl, offset about 65 feet left of centerline, but the ground track was being corrected back toward centerline. A flare was initiated about 600 feet past the runway threshold and about 35 feet agl. During the flare, the ground track achieved the centerline, but deviated back to the left before main gear touchdown, which occurred about 3,200 feet past the runway threshold. At touchdown, the left main gear was about 56 feet left of centerline with an airplane ground track of about 5 degrees to the left. Within 2 seconds of touchdown (about 300 feet of travel), the left main gear crossed the white runway edge strip, and within 5 seconds of touchdown (about 1,000 feet of travel), the left main gear departed the paved surface. A nearly full right rudder input was made at about 3,450 feet from the runway threshold after main gear touchdown. The airplane departed the runway surface before the ground track altered back to the right.
The second in command failed to maintain proper runway alignment, directional control, and landed long. The pilot in command failed to execute a go-around and failed to provide adequate supervision. Additional factors included the thunderstorm, the dark night, the muddy terrain, and the FODed engines.
Accident investigation:
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Investigating agency: | NTSB |
Report number: | CHI01FA292 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
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Sources:
NTSB
History of this aircraft
Other occurrences involving this aircraft Location
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