ASN Wikibase Occurrence # 322817
Date: | Sunday 18 May 2003 |
Time: | 09:35 |
Type: | Beechcraft 300 Super King Air 350 |
Owner/operator: | Oso-Rio LLC |
Registration: | N2SM |
MSN: | FL-24 |
Year of manufacture: | 1990 |
Engine model: | Pratt & Whitney Canada PT6A-60A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed, written off |
Category: | Accident |
Location: | Houston-West Houston Airport, TX (IWS) -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Houston-William P. Hobby Airport, TX (HOU/KHOU) |
Destination airport: | Houston-West Houston Airport, TX (IWS/KIWS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A Beechcraft 300 Super King Air 350, N2SM, was substantially damaged during a runway overrun while landing on runway 33 at the Houston-West Houston Airport, TX (IWS). The airline transport pilot, who was the sole occupant of the airplane, received minor injuries. Visual meteorological conditions prevailed for the personal flight, and a flight plan was not filed. The flight departed Houston-William P. Hobby Airport, TX (HOU) at approximately 09:15.
The pilot reported that while on the base leg, the annunciator light for the "low pitch stop" propeller system on the right side illuminated. The pilot pulled the circuit breaker and left it out, as per the pilot operating handbook (POH). During the landing-roll, the pilot encountered a severe yaw to the right. The pilot added power to the right engine and realigned the airplane down the centerline. He then applied brakes and reverse thrust. The pilot stated that " it felt like I had no braking action and then felt the right side grab and brake, but not the left." The combination of right side braking and the right low pitch system malfunction caused considerable adverse yaw, jerking the plane to the right. The pilot applied power again and straightened the nose of the airplane. He then made the decision to go around, but at this point did not have adequate airspeed or runway length to safely accomplish a go around. He applied the brakes again, and the airplane immediately yawed to the right again, at which time the pilot was unable to compensate before the airplane caught the edge of the runway. The airplane went into the grass, where the pilot attempted to control the direction of the airplane and bring it to a complete stop. Examination of the hydraulic brake hoses from the left and right main landing gears revealed that both hoses appeared to have been damaged with a hand tool.
PROBABLE CAUSE: "The severed hydraulic brake hoses induced a loss of braking action, which resulted in the pilot's failure to control the aircraft."
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | FTW03LA154 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
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