ASN Wikibase Occurrence # 34739
Last updated: 18 June 2013
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| Date: | 16-APR-1982 |
| Time: | 1550 |
| Type: |  Mooney M20J |
| Operator: | private |
| Registration: | N3201P |
| C/n / msn: | 240568 |
| Fatalities: | Fatalities: 3 / Occupants: 3 |
| Other fatalities: | 0 |
| Airplane damage: | Written off (damaged beyond repair) |
| Location: | Bird Island, MN -
United States of America
|
| Phase: | En route |
| Nature: | Executive |
| Departure airport: | Thief River Fal, MN (TVF) |
| Destination airport: | New Ulm, MN (ULM) |
Narrative:THE AIRCRAFT DEPARTED THIEF RIVERS, MN AND PROCEEDED EN ROUTE TO NEW ULM, MN. ONE WITNESS NEAR THE ACCIDENT SITE HEARD A NOISE THAT SOUNDED TO HIM LIKE AN EXPLOSION. HE AND OTHER WITNESSES IN THE VICINITY SAW THE AIRCRAFT DESCENDING OUT OF CONTROL IN A ROLL OR A SPIN BEFORE IT CRASHED. ALSO, THEY SAW TWO OBJECTS FALLING FROM THE AIRCRAFT, ONE SMALL AND ONE LARGE. AN INVESTIGATION REVEALED THAT A PROPELLER BLADE, AND THEN THE ENGINE, HAD SEPARATED IN FLIGHT. THE PROPELLER BLADE WAS FOUND ABOUT TWO WEEKS LATER APPROXIMATELY 1/4 MILE LEFT OF THE FLIGHT PATH. AN EXAMINATION REVEALED THAT THE PROPELLER BLADE HAD FAILED FROM FATIGUE CRACKING. THE FATIGUE ORIGINATED FROM A 1/16 INCH DEEP FORGING FOLD IN THE SURFACE OF THE BLADE NEAR THE BUTT END. THE PROPELLER, A MCCAULEY MODEL 90DHB-16E, HAD 340 HRS TOTAL FLIGHT TIME. CAUSE:
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20020917X01890
Revision history:| Date/time | Contributor | Updates |
| 24-Oct-2008 10:30 |
ASN archive |
Added |
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