ASN Wikibase Occurrence # 35723
Last updated: 19 May 2013
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Date:28-SEP-1989
Time:1400
Type:Silhouette image of generic AS50 model; specific model in this crash may look slightly different
Aérospatiale AS 350D
Operator:Dooley Helicopters
Registration: N57689
C/n / msn: 1312
Fatalities:Fatalities: 1 / Occupants: 1
Other fatalities:0
Airplane damage: Written off (damaged beyond repair)
Location:Chamblee, GA -   United States of America
Phase: Landing
Nature:Ferry/positioning
Departure airport:Rome, GA
Destination airport:Chamblee, GA (PDK)
Narrative:
AS THE HELICOPTER APPROACHED THE AIRPORT, IT WAS OBSERVED TO PITCH UP & YAW UNCONTROLLABLY. ACCORDING TO WITNESSES, THE ROTOR SYSTEM SLOWED AS THE HELICOPTER DESCENDED TO IMPACT ON A CITY GOLF COURSE. AN INVESTIGATION REVEALED THAT THE MAIN ROTOR SWASHPLATE BEARING HAD FAILED FROM INADEQUATE LUBRICATION. THE STATIONARY SWASHPLATE VENTING HOLE HAD NOT BEEN BLOCKED OFF IN ACCORDANCE WITH AEROSPATIALE SVC BULLETIN #62.02. THE PURPOSE OF THE SVC BULLETIN WAS TO PREVENT LEAKAGE OF THE LUBRICANT. THE SWASHPLATE BEARING HAD BEEN LUBRICATED 249 HRS PRIOR TO THE ACCIDENT. PRIORITY AD 89-21-01 WAS ISSUED TO REDUCE THE LUBRICATION INTERVAL FROM 400 TO 100 HOURS & TO BLOCK THE VENT HOLE IN THE STATIONARY SWASHPLATE. THE FUEL FLOW CONTROL LEVER & FUEL SHUT-OFF CONTROL WERE FOUND IN THE CLOSED POSITION (AS IF THE PLT HAD SHUT DOWN THE ENG BEFORE THE ACDNT). CAUSE: FAILURE OF THE MAIN ROTOR SWASHPLATE BEARING DUE TO LACK OF LUBRICANT.

Sources:
NTSB: http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001213X29293


Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
Number of views: 644

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