ASN Wikibase Occurrence # 36435
Last updated: 18 June 2013
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| Date: | 14-FEB-1983 |
| Time: | 2210 |
| Type: |  Cessna 310K |
| Operator: | private |
| Registration: | N6916L |
| C/n / msn: | 310K0016 |
| Fatalities: | Fatalities: 1 / Occupants: 1 |
| Other fatalities: | 0 |
| Airplane damage: | Written off (damaged beyond repair) |
| Location: | Andrews, TX -
United States of America
|
| Phase: | En route |
| Nature: | Private |
| Departure airport: | |
| Destination airport: | Midland, TX (MAF) |
Narrative:THE PLT HAD RECEIVED A WX BRIEFING FOR A FLT TO MILAND, TX. A WITNESS REPORTED THAT AFTER TAKING OFF, HE MADE 2 OR 3 TOUCH-AND-GO LANDINGS. DURING TAKEOFF FROM THE LAST TOUCH-AND-GO, WITNESSES OBSERVED THE ACFT PULL UP ABRUPTLY, ENTER A STEEP RIGHT BANK, THEN CRASH & BURN. AN EXAM OF THE CRASH SITE REVEALED THAT THE ACFT IMPACTED IN A NEAR VERTICAL NOSE DOWN ATTITUDE. BOTH PROP BLADES HAD EVIDENCE OF HIGH ROTATIONAL DAMAGE. THE ELEVATOR TRIM TAB WAS FOUND DEFECTED 15 DEG DOWNWARD (NOSE UP TRIM). THE ELEVATOR TRIM ACTUATOR WAS FOUND EXTENDED 1.1 INCHES. NO PREIMPACT PART FAILURE OR MALFUNCTION WAS FOUND. CAUSE:
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001214X42193
Revision history:| Date/time | Contributor | Updates |
| 24-Oct-2008 10:30 |
ASN archive |
Added |
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