ASN Wikibase Occurrence # 37743
Last updated: 19 June 2013
This information is added by users of ASN. ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
| Date: | 07-AUG-1993 |
| Time: | 1345 |
| Type: | Midget Mustang |
| Operator: | private |
| Registration: | C-FYSJ |
| C/n / msn: | 517 |
| Fatalities: | Fatalities: 1 / Occupants: 1 |
| Other fatalities: | 0 |
| Airplane damage: | Substantial |
| Location: | Wadesboro, NC -
United States of America
|
| Phase: | En route |
| Nature: | Private |
| Departure airport: | Siler City, NC (5W8) |
| Destination airport: | Jacksonville, FL (CRG) |
Narrative:WITNESSES HEARD THE SOUND OF A DIVING AIRPLANE, THEN OBSERVED A FRAGMENTED AIRPLANE FALLING OUT OF THE CLOUDS AND CONTINUING IN A NOSE-LOW ATTITUDE UNTIL IMPACT WITH TERRAIN. THE CANADIAN REGISTERED HOMEBUILT PLANE HAD BEEN PURCHASED BY THE PILOT TWO DAYS BEFORE THE ACCIDENT. THE PILOT RECEIVED A WEATHER BRIEFING FROM RALEIGH AUTOMATED FLIGHT SERVICE STATION THE DAY OF THE ACCIDENT WHICH CALLED FOR INSTRUMENT METEOROLOGICAL CONDITIONS ALONG THE PROPOSED ROUTE OF FLIGHT. OFFICIAL TRANSCRIPTS FROM THE TELEPHONE CONVERSATION BETWEEN THE PILOT AND FLIGHT SERVICE CONTAIN STATEMENTS MADE BY THE PILOT ACKNOWLEDGING THE FACT THAT THE AIRPLANE DID NOT HAVE THE PROPER INSTRUMENTATION FOR FLIGHT INTO IMC CONDITIONS, BUT THAT HE PLANNED TO ATTEMPT THE FLIGHT ANYWAY. CAUSE: THE PILOT'S INTENTIONAL FLIGHT INTO IMC WITHOUT THE PROPER INSTRUMENTATION, WHICH RESULTED IN THE PILOT'S LOSS OF AIRCRAFT CONTROL, AND IN FLIGHT BREAKUP OF THE AIRPLANE.
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001211X13060
Revision history:| Date/time | Contributor | Updates |
| 24-Oct-2008 10:30 |
ASN archive |
Added |
Number of views: 637