ASN Wikibase Occurrence # 39107
Last updated: 19 June 2013
This information is added by users of ASN. ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.
Date:30-JAN-1983
Time:0720
Type:Taylorcraft BC-12D
Operator:private
Registration: N95176
C/n / msn: 9576
Fatalities:Fatalities: 1 / Occupants: 2
Other fatalities:0
Airplane damage: Written off (damaged beyond repair)
Location:Alton, ME -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:
Destination airport:Ross Lake, ME
Narrative:
THE PAX STATED THAT THE FUSELAGE & RIGHT WING TANKS CONTAINED AUTOMOTIVE FUEL. THE ENG WAS WARMED UP AN ESTIMATED 30 MINPRIOR TO TAKEOFF. THE ACFT WAS OBSERVED TO LIFT OFF ABOUT 1/2 WAY DOWN THE 1600 FT STRIP. AT ABOUT 30-40 FT THE ACFT BEGAN A RIGHT BANKING TURN. THE PAX STATED THAT AT ABOUT 75 FT ABOVE THE TREES THE Engine quit. THE PLT TURNED THE ACFT LEFT BACK TOWARD THE RWY, & THE PAX OBSERVED THE PLT PULLING & PUSHING A KNOB. THE ACFT CRASHED IN A NEAR VERTICAL NOSE DOWN ATTITUDE. THE PLT'S LOGBOOK INDICATED A TOTAL OF 11.9 HRS DUAL WITH THE LAST DUAL ON 7/24/81. THE LAST RECORDED ANNUAL WAS ON 3/31/81 WHICH COULD NOT BE SIGNED OFF BECAUSE AN STC INVOLVING AN ENG CHANGE WAS NOT COMPLETED. THE ACFT WAS EQUIPPED WITH SKIS & THEIR INSTALLATION WAS NOT RECORDED IN THE LOGBOOK. THE ACFT WAS ABOUT 175 LBS OVER MAX GROSS WEIGHT AT THE TIME OF THE ACCIDENT. OAT AT BANGOR, ME WAS 20 DEG F. RECENT TESTS SHOW THAT A CARBURETOR HAD A TENDENCY TO COMMENCE ICING TWICE AS SOON WITH AUTOMOTIVE GRADE FUEL AS COMPARED WITH 100LL AVIATION GRADE. CAUSE:

Sources:
NTSB: http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001214X42075


Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
Number of views: 536

Corrections or additions? ... Edit this accident description