ASN Wikibase Occurrence # 44712
Last updated: 22 May 2013
This information is added by users of ASN. ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.
Date:06-SEP-2004
Time:1010
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different
Mooney M20D
Operator:
Registration: N1907Y
C/n / msn: 202
Fatalities:Fatalities: 1 / Occupants: 1
Other fatalities:0
Airplane damage: Written off (damaged beyond repair)
Location:Pagosa Springs, CO -   United States of America
Phase: Take off
Nature:Private
Departure airport:Pagosa Springs, CO (2V1)
Destination airport:Durango, CO (DRO)
Narrative:
The pilot and his wife made several attempts to take off but aborted each one. Airport personnel said that when the pilot came into the office, he appeared thoroughly shaken by the experience. He told employees he would not take off from the airport until runway construction had been completed and entire length of the runway was made available. He also told a mechanic that there was a shimmy in the nose wheel steering. He contracted with a local flight instructor to deliver the airplane after the repairs had been made. Delivery was postponed on three different occasions and over a period of two months when discrepancies were discovered: the right fuel tank leaked and the VOR receivers did not work; instead of being mounted on the windshield center post, the magnetic compass dangled by a few wires underneath the instrument panel, and the airspeed indicator was twisted about 60 degrees in the instrument panel. The fuel cap O-rings were "severely cracked and worn." The communication radios stopped working, the battery required charging, and the airplane required a jump-start. There were numerous 9-volt and AA batteries on the rear floor and in the door pockets. The flight instructor elected not to deliver the airplane. The pilot elected to ferry the airplane home. During the takeoff roll, the airplane departed the left side of the runway and skipped across the ground before striking a 600-pound concrete block and coming to rest inverted. A post-impact fire ensued. The 9,000-foot runway was undergoing reconstruction and only 3,900 feet was available. An additional 600-foot displaced threshold was available for takeoffs. The useable portion of runway was rough and uneven.

CAUSE: the pilot's inadequate preflight planning and his failure to maintain directional control. Contributing factors were the pilot's failure to abort the takeoff, and the rough and uneven runway surface.

Sources:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20040910X01386&key=1


Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
Number of views: 561

Corrections or additions? ... Edit this accident description