ASN Wikibase Occurrence # 324094
Date: | Tuesday 25 November 1997 |
Time: | 08:13 |
Type: | Shorts 360-100 |
Owner/operator: | Corporate Air |
Registration: | N691A |
MSN: | SH.3618 |
Year of manufacture: | 1983 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial, written off |
Category: | Accident |
Location: | Billings-Logan International Airport, MT (BIL) -
United States of America
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Phase: | Landing |
Nature: | Cargo |
Departure airport: | Great Falls International Airport, MT (GTF/KGTF) |
Destination airport: | Billings-Logan International Airport, MT (BIL/KBIL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A Short 360, N691A, operated by Corporate Air, was substantially damaged when the left main landing gear collapsed on landing at the Billings-Logan International Airport, MT (BIL). Both pilots were uninjured. Instrument meteorological conditions existed at the time, and an IFR flight plan was in effect. The flight, which was an unscheduled, domestic cargo flight from Great Falls International Airport, MT (GTF) departed approximately 07:15.
The cargo flight was being vectored for the VOR/DME RWY 28R approach to Billings during instrument meteorological conditions. Weather conditions one minute before the accident were winds 020 at 13 knots, light snow and mist, and visibility was deteriorating rapidly. The co-pilot was flying the aircraft, and the PIC was handling radio communications. At 08:12, having crossed the final approach fix, the aircraft descended through 100 feet above the MDA (3,940 feet or 426 feet above the runway threshold), and immediately thereafter the crew visually acquired the runway. At 08:13 the aircraft's GPWS alert of 'SINK RATE' was heard, followed 2 seconds later by the PIC calling for 'POWER,' and a 2 second delay to ground impact. The co-pilot had logged a total of 103 hours in the Shorts 360 all within the previous 90 days, while the PIC had just begun flying the aircraft in Montana's late fall weather after a 6 year assignment flying in the Hawaiian islands. The left main landing gear collapsed in overload during the ground impact.
PROBABLE CAUSE: "The co-pilot's failure to maintain the proper descent rate on final approach, the pilot-in-command's delayed remedial action, and overload of the left main landing gear assembly. Factors contributing were snow, crosswind conditions and deteriorating visibility."
Accident investigation:
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Investigating agency: | NTSB |
Report number: | SEA98LA016 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
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Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
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