ASN Wikibase Occurrence # 320357
Date: | Monday 9 February 2015 |
Time: | 22:07 |
Type: | Embraer ERJ-190AR (ERJ-190-100 IGW) |
Owner/operator: | US Airways |
Registration: | N953UW |
MSN: | 19000133 |
Year of manufacture: | 2007 |
Total airframe hrs: | 16216 hours |
Engine model: | General Electric CR3410E6 |
Fatalities: | Fatalities: 0 / Occupants: 56 |
Aircraft damage: | Substantial, repaired |
Category: | Accident |
Location: | Houston-George Bush Intercontinental Airport, TX (IAH) -
United States of America
|
Phase: | Landing |
Nature: | Passenger - Scheduled |
Departure airport: | Philadelphia International Airport, PA (PHL/KPHL) |
Destination airport: | Houston-George Bush Intercontinental Airport, TX (IAH/KIAH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:US Airways flight 1825, an Embraer ERJ-190, landed with the nose landing gear not extended at the Houston-George Bush Intercontinental Airport (IAH), Texas, USA. The 4 crew and 51 passengers were not injured; one passenger received minor injuries during the subsequent airplane evacuation.
The flight departed Philadelphia International Airport (PHL), Pennsylvania, about 17:06. The crew reported that when they placed the landing gear lever in the down position near IAH, they received amber caution and red warning messages on the engine indication and crew alerting system. After accomplishing quick reference handbook items, the crew could not determine the position of the landing gear and conducted two passes by the air traffic control tower; tower personnel indicated that the nose landing gear (NLG) was not down. The crew declared an emergency, and the captain landed the airplane on runway 27 with the NLG retracted; the forward fuselage contacted the runway, and the flight deck filled with smoke. An evacuation was carried out.
Probable cause: "An undetermined malfunction of the nosewheel steering control module, which resulted in the nose landing gear being jammed in the gear bay. Contributing to the accident was the improper rigging of the nosewheel steering feedback sensors during installation."
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN15LA140 |
Status: | Investigation completed |
Duration: | 6 years and 2 months |
Download report: | Final report |
|
Sources:
NTSB CEN15LA140
History of this aircraft
Other occurrences involving this aircraft
31 March 2019 |
N953UW |
American Airlines |
0 |
Boston-Logan International Airport, MA (BOS/KBOS) |
|
unk |
Bird strike |
Location
Revision history:
Date/time | Contributor | Updates |
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