ASN Wikibase Occurrence # 134286
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 9 November 2001 |
Time: | 14:45 |
Type: | Agusta A119 Koala |
Owner/operator: | Ihc Life Flight |
Registration: | N119RX |
MSN: | 14014 |
Year of manufacture: | 2001 |
Total airframe hrs: | 40 hours |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Ogden, UT -
United States of America
|
Phase: | Landing |
Nature: | Executive |
Departure airport: | Salt Lake City, UT (SLC) |
Destination airport: | Ogden, UT |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Prior to accepting delivery of the new helicopter, the pilot noticed a 4 percent decay in rotor rpm when the collective control was lowered after landing, activating the aural and visual LOW ROTOR RPM warnings. After a few seconds, engine and rotor speed returned to normal. The engine manufacturer said it should be of no concern as long as it operated normally during flight, but suggested adjusting the linear variable differential transducer after they ferried the helicopter home. On the day of the accident, the pilot intended to make a low pass and land at a hospital helipad. He lowered the collective control and noticed rotor rpm had decreased to 96 percent. The LOW ROTOR RPM warnings activated. He realized he was too low to attempt an autorotation. He reduced collective and pitch attitude further. RPM drooped to 90 percent, and stabilized. Approximately 20 to 30 feet above the helipad, the pilot raised the collective control to flare for landing. RPM rapidly deteriorated. The aircraft impacted the helipad in a tail-down position, rolled over, and came to rest on its left side. The operator found the rotary variable differential transformer rigged at 57.9 degrees of twist grip travel at the Flight Gate position. According to the A119 maintenance manual, the device is supposed to be rigged to achieve 60 degree ( or - 1 degree). The operator said misrigging of the rotary variable differential transducer would cause incorrect fuel scheduling to the fuel control unit.
Probable Cause: improper rigging of the rotary variable differential transformer by the manufacturer, resulting in incorrect fuel scheduling to the fuel control unit.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN02LA010 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20011204X02353&key=1 Revision history:
Date/time | Contributor | Updates |
29-Jan-2013 12:52 |
TB |
Updated [Aircraft type, Operator, Departure airport, Destination airport, Source, Narrative] |
13-May-2013 03:59 |
Anon. |
Updated [Source] |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Dec-2017 13:17 |
ASN Update Bot |
Updated [Operator, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation