ASN Wikibase Occurrence # 146210
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Date: | Thursday 7 June 2012 |
Time: | 16:15 |
Type: | Beechcraft 77 Skipper |
Owner/operator: | Private |
Registration: | N18012 |
MSN: | WA-276 |
Engine model: | Lycoming O-235 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Clark, SD -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Pierre, SD (PIR) |
Destination airport: | Morris, MN (MOX) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The passenger reported that the airplane’s low fuel light illuminated during the flight. She stated that they continued the flight and were circling to land on a grass runway when the airplane crashed. A witness reported seeing the airplane pass over the runway at a low altitude with the engine operating. The airplane then abruptly climbed and initiated a turn. The witness said that the airplane’s nose dropped as if the airplane had stalled and it then descended and impacted the ground. The airplane incurred substantial damage, which included separation of the engine, outboard left wing and aft fuselage, and upward bending of the right wing. There was no bending of the blades of the engine’s propeller, indicating that the engine was not producing power at the time of the impact. Both fuel tanks ruptured, and only 1 gallon of fuel was recovered at the scene. No fuel was found in the gascolator or carburetor. No fuel odor was present at the accident site. The airplane maintenance manual indicated that 1 gallon of the airplane’s fuel supply was unusable fuel. It is likely that the engine lost power during the landing approach due to fuel exhaustion and that the pilot failed to maintain airspeed after the power loss, resulting in an inadvertent stall.
Probable Cause: The pilot’s improper fuel management, which led to fuel exhaustion, and his failure to maintain adequate airspeed resulting in an aerodynamic stall.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN12LA346 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
08-Jun-2012 13:47 |
Geno |
Added |
08-Jun-2012 15:44 |
RobertMB |
Updated [Aircraft type, Source, Narrative] |
08-Jun-2012 23:00 |
Anon. |
Updated [Aircraft type, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:46 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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