Loss of control Accident Steen Skybolt N863SB,
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ASN Wikibase Occurrence # 166824
 
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Date:Sunday 8 June 2014
Time:15:40
Type:Silhouette image of generic BOLT model; specific model in this crash may look slightly different    
Steen Skybolt
Owner/operator:Private
Registration: N863SB
MSN: 01
Year of manufacture:2000
Engine model:Continental IO-470 SER
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Whifferdill Airport (TN77), Chapmansboro, TN -   United States of America
Phase: Take off
Nature:Private
Departure airport:Chapmansboro, TN (TN77)
Destination airport:Chapmansboro, TN (TN77)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that he performed a preflight inspection with no anomalies noted. In addition, he performed an engine run-up, and everything was normal. During the initial climb, about 200 ft above ground level and just over the departure end of the runway, the pilot noticed that the airplane was not producing full power; witnesses corroborated that the engine lost partial power after the airplane reached the end of the runway. The pilot chose to return to the runway and performed a 180-degree turn. Once the airplane was over the runway centerline, the pilot attempted to add power; however, the engine did not respond. Witnesses reported that, as the airplane neared the runway, the pilot “flared too high” and that the airplane then “stalled,” descended, and impacted the runway. A postimpact fire ensued. A postaccident examination of the engine revealed no evidence of mechanical failures or malfunctions that would have precluded normal operation. The reason for the partial loss of engine power could not be determined.

Probable Cause: The pilot's failure to maintain airspeed while performing an emergency landing, which led to the airplane exceeding its critical angle-of-attack and experiencing a subsequent aerodynamic stall. Contributing to the accident was a partial loss of engine power for reasons that could not be determined during postaccident examinations.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA14LA281
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=863SB

Location

Revision history:

Date/timeContributorUpdates
09-Jun-2014 18:01 gerard57 Added
09-Jun-2014 18:02 harro Updated [Aircraft type, Registration, Cn, Location]
12-Jun-2014 04:45 Geno Updated [Time, Location, Departure airport, Source, Narrative]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
29-Nov-2017 15:02 ASN Update Bot Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative]

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