ASN Wikibase Occurrence # 167534
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Date: | Saturday 21 June 2014 |
Time: | 10:30 |
Type: | RotorWay Exec 162F |
Owner/operator: | Tim G Payne |
Registration: | N6828D |
MSN: | 6460 |
Year of manufacture: | 2000 |
Engine model: | ROTORWAY RW-145 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Indianapolis Regional Airport (KMQJ), Indianapolis, IN -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Mt. Comfort, IN (MQJ) |
Destination airport: | Goshen, IN (GSH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, while the experimental, amateur-built helicopter was climbing through 300 feet, he heard a loud “bang” come from the rear compartment and that the helicopter subsequently yawed right. He made an emergency autorotation landing to a field. During the landing, the helicopter’s skids sunk into the mud, and the main rotor blades contacted the ground. The helicopter then came to rest on its side. A postaccident examination of the helicopter revealed that the main rotor belt was not approved for aircraft use and that it was broken straight across in a crimp-type failure. According to the belt manufacturer, belt crimping damage is “commonly associated with belt mishandling, inadequate belt installation tension, sub-minimal sprocket diameters, and/or entry of foreign objects within the belt drive.” No foreign object preimpact damage was found. Further, although the belt was an unapproved part, it should have been inspected during each 25-hour standard inspection and the belt tension was to be tested during each annual inspection. At the time of the accident, the belt had accumulated 215.9 total hours. Based on this evidence, the pilot installed an unauthorized main rotor drive belt and then failed to properly inspect the belt, which resulted in inadequate belt tension, the belt’s failure, and the subsequent loss of engine power.
Probable Cause: The pilot’s installation of an unauthorized main rotor belt and his subsequent failure to properly inspect the belt, which resulted in inadequate belt tension, the belt’s failure, and the subsequent loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN14LA307 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N6828D Location
Revision history:
Date/time | Contributor | Updates |
26-Jun-2014 04:24 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 15:03 |
ASN Update Bot |
Updated [Operator, Departure airport, Destination airport, Source, Narrative] |
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