Accident Ayres S-2R-G6 Turbo Thrush N61374,
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ASN Wikibase Occurrence # 21556
 
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Date:Friday 20 June 2008
Time:14:00
Type:Silhouette image of generic SS2T model; specific model in this crash may look slightly different    
Ayres S-2R-G6 Turbo Thrush
Owner/operator:Swan Lake Flying Service, Inc.
Registration: N61374
MSN: G6-119
Total airframe hrs:7040 hours
Engine model:Garrett TPE-331-G6
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Pine Bluff, AR -   United States of America
Phase: En route
Nature:Agricultural
Departure airport:Altheimer, AR
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot was spraying a rice field with fertilizer when the "airplane began to lose altitude." The pilot attempted a forced landing in an open bean field. During the forced landing the airplane's right wing struck a tree, spinning the airplane around to the right. The airplane then impacted the terrain sideways, shearing off the landing gear, bending both wings, and buckling the fuselage. An examination of the engine showed evidence indicating the engine was not operating prior to impact. Additionally, the examination showed nothing that would have caused a loss of power or an in-flight engine shutdown. Further investigation determined that the airplane had previously experienced an uncommanded engine shut down. According to the wiring system schematic, the manufacturer did not install engine speed switches to automatically and electronically control the fuel system, but instead, installed pilot-activated switches for manual control of the fuel system. Examination of the system showed evidence of a short in the wires to the switch. The manufacturer stated that if a short in the wires occurred or if a switch failed due to contamination or corrosion, voltage could be sent to pin "B" on the Fuel Shutoff (Solenoid) Valve, causing the fuel shutoff valve to close.
Probable Cause: A total loss of engine power due to fuel starvation as a result of an electrical short in the wiring to the manual fuel switch that closed the fuel valves.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN08LA107
Status: Investigation completed
Duration: 1 year 1 month
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
05-Jul-2008 12:28 Fusko Added
21-Dec-2016 19:14 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:16 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:20 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
03-Dec-2017 11:21 ASN Update Bot Updated [Other fatalities, Departure airport, Source, Narrative]

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