ASN Wikibase Occurrence # 21603
This record has been locked for editing.
Date: | Saturday 5 July 2008 |
Time: | 20:00 |
Type: | Van's RV-8 |
Owner/operator: | Private |
Registration: | N184KS |
MSN: | 80874 |
Engine model: | Lycoming IO-360 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | T-Bone Ranch, near Valera, TX -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Coleman, TX (KCOM) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was performing low passes over a private ranch. The airplane was fueled the day before the accident with 17.4 gallons of fuel and had a 42-gallon fuel capacity. The pilot had commented to his wife prior to the accident that he didn't want a full fuel load for the flyover. After the pilot refueled, he flew the airplane for at least an hour that day and for an undetermined amount of time the day of the flyover. The pilot planned for and flew three low-altitude passes, ending each pass with a pull-up. During the pull-up from the third pass, the airplane was seen to roll to the left followed by a steep dive into a car parking area. The airplane turned approximately 270 degrees from the start of the pull-up until it impacted the ground. An examination of the airplane showed no evidence of aviation fuel at the accident site, in the airplane's fuel tanks, or in the engine fuel lines. The propeller and engine case damage was consistent with that of an engine not developing power at impact. The engine manual states that the engine burn rate is approximately 9.5 gallons per hour in economy cruise flight and 12.3 gallons per hour in performance cruise flight.
Probable Cause: The pilot's failure to maintain adequate airspeed, which led to an aerodynamic stall, following a loss of engine power due to fuel exhaustion. Contributing to the accident was the pilot's mismanagement of fuel and the low altitude at which the fuel loss occurred.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN08LA119 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
07-Jul-2008 12:03 |
Fusko |
Added |
07-Jul-2008 12:22 |
harro |
Updated |
17-Jul-2008 10:25 |
Fusko |
Updated |
27-Nov-2016 18:14 |
junior sjc |
Updated [Operator, Destination airport, Narrative] |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 11:26 |
ASN Update Bot |
Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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