Accident Flight Design CTLS N81KK,
ASN logo
ASN Wikibase Occurrence # 223615
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Saturday 30 March 2019
Time:15:59 LT
Type:Silhouette image of generic FDCT model; specific model in this crash may look slightly different    
Flight Design CTLS
Owner/operator:Bailey Florida LLC
Registration: N81KK
MSN: 07-12-03
Year of manufacture:2008
Total airframe hrs:627 hours
Engine model:Rotax 912 ULS
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Putnam County near Bostwick, FL -   United States of America
Phase: En route
Nature:Private
Departure airport:Hilton Head Airport, SC (HHH/KHXD)
Destination airport:Palatka, FL (28J)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that the cross-country flight was uneventful until he was approaching the destination airport from the north, when the engine lost total power. He was unable to restart the engine and prepared for a forced landing in a clearing. He deployed the airplane's Ballistic Recovery System (BRS); the rocket fired, but the parachute remained in its container. During the forced landing, the airplane was substantial damage and the pilot and passenger were seriously injured.

The pilot reported that he began the flight with about 13.5 gallons of fuel on board, which was consistent with the recorded fuel quantity remaining indicated by the airplane's engine monitoring system (EMS); however, this value was not directly measured and depended on pilot input. There was no odor of fuel or evidence of fuel leaks at the crash site. The fuel tanks were not compromised during the impact and no fuel was found in the fuel tanks during recovery.

The engine and fuel system were examined after the accident and a test run was performed. The engine ran normally on the airframe and no evidence of a preexisting mechanical failure or anomaly was found. Examination of the EMS data revealed that, during the power loss, fuel flow increased to more than twice the normal rate. According to the engine manufacturer, air introduced into the fuel system due to fuel exhaustion can result in a fuel flow increase due to the impeller on the fuel flow transducer speeding up. Given this information, it is likely that the initial fuel-on-board indications were incorrect (as they were not indications, but calculations based on pilot input) and that the loss of engine power was the result of fuel exhaustion.

An examination of the BRS revealed numerous conditions that were indicative of improper or nonexistent maintenance and inspections. These conditions, among others, included the following. The S-folded harnesses were improperly secured inside the egress panel. These harnesses improperly protruded into and blocked the egress opening. They also protruded into and blocked the opening of the parachute canister. During the attempted BRS deployment, a portion of the egress panel remained attached to the airframe due to improper bonding. This condition blocked the parachute container, caused the rocket to deflect from its intended trajectory and resulted in the failure of the parachute to deploy.

The unairworthy condition of the BRS would have been prevented with proper preventative maintenance and use of the pilot's preflight inspection procedures for the BRS. A review of the aircraft maintenance logbooks showed no compliance with an airframe manufacturer's service bulletin that would have corrected these conditions if properly accomplished. Also, several of the airworthiness issues with the BRS could have been captured if the pilot's preflight procedures for the BRS had been properly performed.

Finally, the EMS data revealed that the pilot allowed the airspeed to decay below best glide speed during the final minute of flight before ground impact. Thus, the vertical speed of the airplane increased and most likely resulted in greater damage and injury versus maintaining best glide speed throughout the forced landing.
 

Probable Cause: The pilot's improper management of his fuel supply, which resulted in fuel exhaustion and a total loss of engine power. Contributing to the outcome was the improper maintenance of the airplane's ballistic recovery parachute system, which resulted in its failure to properly deploy. Also contributing, was the pilot's failure to maintain the proper glide speed through the subsequent forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA19LA141
Status: Investigation completed
Duration: 3 years 1 month
Download report: Final report

Sources:

NTSB ERA19LA141

FAA register: https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=81KK

Location

Revision history:

Date/timeContributorUpdates
30-Mar-2019 22:31 Geno Added
31-Mar-2019 01:04 RobertMB Updated [Aircraft type, Registration, Cn, Operator, Source]
02-Jul-2022 09:32 ASN Update Bot Updated [Time, Cn, Other fatalities, Nature, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org