Accident Fantasy Allegro 2000 N5020X,
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ASN Wikibase Occurrence # 228206
 
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Date:Wednesday 14 August 2019
Time:07:41 LT
Type:Silhouette image of generic ALGR model; specific model in this crash may look slightly different    
Fantasy Allegro 2000
Owner/operator:Private
Registration: N5020X
MSN: 05-216
Year of manufacture:2005
Engine model:Rotax 912UL
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:between Todd and Deep Gap, Watauga County, NC -   United States of America
Phase: Approach
Nature:Private
Departure airport:Boone, NC
Destination airport:Boone, NC
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Several witnesses noted the airplane was flying but did not hear an engine sound while it was in the traffic pattern of an airstrip adjacent to the pilot's house. Witnesses reported hearing the airplane impact terrain. A postcrash fire occurred. The pilot was able to self-extricate himself and informed a first responder and medical personnel that he was "circling to land and the engine bogged down."

Examination of the wreckage found the cockpit and inboard portions of the wings were consumed by the postcrash fire; there was no evidence of preimpact failure or malfunction of the flight controls for roll, pitch, and yaw. Examination of the engine revealed no evidence of failure or malfunction of the powertrain, but heat damage to the fuel metering, ignition, and cooling systems precluded determining whether there was any preexisting issue with those systems.

While the pilot's autopsy found severe atherosclerotic coronary artery disease, he initially survived the accident and did not experience a loss of consciousness; thus, sudden incapacitation was not a factor. Medication found in his system was the result of postaccident medical intervention. Personal medical records revealed that the pilot had a stroke about 2 months prior to the crash that resulted in the loss of his right visual fields. The condition, called homonymous hemianopsia, causes difficulty in visual-motor control and perception in space. However, without knowledge of the intended flight pattern and timing of the reported loss of engine power, it could not be determined whether the pilot's homonymous hemianopsia contributed to the accident.

Probable Cause: The reported total loss of engine power for reasons that could not be determined based on the available evidence.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA19LA247
Status: Investigation completed
Duration: 2 years and 7 months
Download report: Final report

Sources:

NTSB ERA19LA247
FAA register: https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=5020X


Location

Media:

Revision history:

Date/timeContributorUpdates
14-Aug-2019 15:49 Geno Added
14-Aug-2019 17:29 Geno Updated [Aircraft type, Registration, Cn, Operator, Source, Narrative]
15-Aug-2019 12:21 Captain Adam Updated [Total fatalities, Narrative]
15-Aug-2019 15:45 Iceman 29 Updated [Source, Embed code, Damage]
15-Aug-2019 15:56 Iceman 29 Updated [Embed code]
16-Aug-2019 10:05 RobertMB Updated [Registration, Location, Phase, Nature, Source, Narrative]
01-Jul-2022 19:23 ASN Update Bot Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Embed code, Narrative, Category, Accident report]

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