ASN Wikibase Occurrence # 244279
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Date: | Thursday 25 June 2020 |
Time: | 13:40 UTC |
Type: | Cessna F152 (Reims) |
Owner/operator: | Herefordshire Aero Club Ltd |
Registration: | G-BTAL |
MSN: | 1444 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | None |
Location: | Shobdon Airfield, Shobdon, Leominster, Herefordshire -
United Kingdom
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Shobdon Airport (EGBS) |
Destination airport: | Shobdon Airport (EGBS) |
Confidence Rating: | Information verified through data from accident investigation authorities |
Narrative:AAIB investigation to Reims Cessna F152, G-BTAL: Partial engine failure and forced landing, Shobdon Aerodrome, Herefordshire, 25 June 2020. The AAIB Final Report into the incident was published on 10 September 2020, and the following is an excerpt from it:
"The pilot had not flown for several months due to public health restrictions and on the day of the incident was planning to complete three circuits to regain recency. The first two circuits were uneventful. He took off for the third circuit with the flaps up and full power. As the aircraft reached 300 – 400 ft the engine lost all power. The pilot described it feeling like “someone had pulled the throttle to idle”.
He immediately lowered the nose and selected a field slightly to his left. He recalled that the power returned briefly then reduced again but he decided to close the throttle and treat the engine as completely failed. He made a MAYDAY call then focused on the landing.
The pilot landed the aircraft with the flaps up in a slight crosswind. As the aircraft touched down he noticed a ditch crossing the aircraft’s track and decided to pull back on the control column to pass over it. Once clear of the ditch he brought the aircraft to a halt and shut the engine down. The aircraft was not damaged and the pilot was able to exit the
aircraft normally
AAIB Analysis
The pilot attributed the safe outcome to having planned and reviewed his actions in the event of an engine failure prior to taking off. This freed sufficient capacity such that, when the event occurred, he could focus on flying the aircraft. He also treated the partial failure as a complete failure. Having read about previous accidents he was not tempted to turn back and instead selected a field ahead and focused on landing.
The reason for the engine failure was not determined. It is possible it was caused by carburettor icing".
Sources:
1. AAIB Final Report:
https://assets.publishing.service.gov.uk/media/5f3cf7cf8fa8f51749698738/Reims_Cessna_F152_G-BTAL_09-20.pdf 2.
https://www.jetphotos.com/photo/9493708 3.
https://www.flickr.com/photos/vlk77/35052438013 4.
https://abpic.co.uk/pictures/registration/G-BTAL 5.
https://www.airport-data.com/aircraft/photos/G-BTAL:1.html Media:
Reims Cessna F152 G-BTAL at Gloucestershire Airport 19 October 2016:
Revision history:
Date/time | Contributor | Updates |
21-Oct-2020 19:39 |
Dr. John Smith |
Added |
21-Oct-2020 19:40 |
Dr. John Smith |
Updated [Destination airport, Embed code, Narrative] |
23-Oct-2020 23:28 |
Dr. John Smith |
Updated [Embed code] |
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