ASN Wikibase Occurrence # 246778
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 2 September 2016 |
Time: | 17:38 LT |
Type: | ATR 72-600 (72-212A) |
Owner/operator: | Aer Lingus Regional, opb Stobart Air |
Registration: | EI-FAW |
MSN: | 1122 |
Fatalities: | Fatalities: 0 / Occupants: 54 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | 5.5 nm E of Dublin Airport (EIDW) -
Ireland
|
Phase: | Approach |
Nature: | Passenger - Scheduled |
Departure airport: | Edinburgh-Turnhouse Airport (EDI/EGPH) |
Destination airport: | Dublin Airport (DUB/EIDW) |
Investigating agency: | AAIU |
Confidence Rating: | Information verified through data from accident investigation authorities |
Narrative:The aircraft, an ATR 72-600, was approaching Dublin Airport (EIDW) following a scheduled passenger flight from Edinburgh Airport (EGPH) in the United Kingdom. During the intermediate descent prior to commencing the published instrument approach procedure for runway 28, the aircraft descended below the altitude assigned by the Air Traffic Control Officer (ATCO).
The‘Minimum Safe Altitude Warning’ (MSAW) activated on the ATCO’s radar screen to warn the ATCO about the aircraft’s continued descent.
The aircraft had descended to an altitude of 1,082 ft. The altitude of an aircraft at this point on the ILS glideslope for RWY 28 should have been 1,975 ft.
When contacted by the ATCO, the Commander initiated a missed approach, climbed to a safe altitude and obtained radar vectors for a second approach. The aircraft subsequently landed at EIDW without further incident.
Probable Cause:
While conducting an ILS approach, the aircraft was descended unintentionally to an altitude that triggered the ATC Minimum Safe Altitude Warning.
Contributory Cause(s)
1.The Flight Crew’s lack of experience on the ATR72 ‘-600’ aircraft.
2.The Commander became distracted by the manual operation of the TLU to the extent that the flight path was not adequately monitored.
3.There were inappropriate pitch inputs made to the Commander’s control column that caused the autopilot to disengage.
4.The level of cockpit communication and co-ordination between the Flight Crew was sub-optimal
Accident investigation:
|
| |
Investigating agency: | AAIU |
Report number: | |
Status: | Investigation completed |
Duration: | 4 years and 4 months |
Download report: | Final report |
|
Sources:
AAIU
Images:
Figure: AAIU
Figure: AAIU
Revision history:
Date/time | Contributor | Updates |
15-Jan-2021 18:19 |
harro |
Updated [Photo] |
15-Jan-2021 18:21 |
harro |
Updated [Location, Photo] |
15-Jan-2021 19:57 |
Airfish86 |
Updated [Date, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation