ASN Wikibase Occurrence # 253956
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Date: | Sunday 25 April 2021 |
Time: | 10:03 LT |
Type: | Skystar Kitfox Classic IV |
Owner/operator: | Sale Reported |
Registration: | N90KF |
MSN: | C9603-0147 |
Year of manufacture: | 2008 |
Total airframe hrs: | 109 hours |
Engine model: | Rotec Radial R-2800 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | S of Mountain Rest, Oconee County, SC -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Clemson-Oconee County Airport, SC (CEU/KCEU) |
Destination airport: | Mountain Rest, SC |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, while maneuvering at low altitude surveying fields in his experimental, amateur-built airplane, the engine stopped producing power about 600 ft above ground level (agl) and the propeller continued to windmill. He selected a field for a forced landing site, established the best glide speed, and turned on the electric fuel pump, which restored some power to the engine for about 10 seconds. He stated that when he realized that the airplane would not make it to the selected field, he reduced the throttle to idle and performed a forced landing into trees.
Postaccident examination of the engine revealed no evidence of preimpact mechanical malfunctions or failures that would have precluded normal operation; however, the engine was not equipped with carburetor heat as recommended in the engine installation manual.
The weather conditions at the time of the accident were conducive to the formation of serious carburetor icing at cruise power engine power settings. Thus, it is likely that carburetor ice formed and subsequently resulted in the partial loss of engine power during the climb from the low pass over the field. Had carburetor heat been installed on the engine and been used during these low approaches, the ice accumulation likely would have been prevented.
Probable Cause: A partial loss of engine power due to carburetor icing. Contributing to the accident was the engine's lack of carburetor heat.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA21LA192 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
|
Sources:
NTSB ERA21LA192
FAA register:
https://registry.faa.gov/aircraftinquiry/Search/NNumberResult?NNumberTxt=90KF%20 https://flightaware.com/live/flight/N90KF Location
Revision history:
Date/time | Contributor | Updates |
25-Apr-2021 20:32 |
Geno |
Added |
25-Apr-2021 20:36 |
Geno |
Updated [Source, Damage, Narrative] |
25-Apr-2021 20:39 |
Geno |
Updated [Narrative] |
26-Apr-2021 00:46 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Source] |
26-Apr-2021 15:11 |
RobertMB |
Updated [Registration, Location, Phase, Nature, Departure airport, Destination airport, Source, Damage, Narrative] |
27-Apr-2021 02:35 |
Captain Adam |
Updated [Narrative] |
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