Accident Mooney M20C Ranger N6448U,
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ASN Wikibase Occurrence # 254049
 
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Date:Thursday 29 April 2021
Time:12:17 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20C Ranger
Owner/operator:Private
Registration: N6448U
MSN: 2195
Year of manufacture:1962
Total airframe hrs:5091 hours
Engine model:Lycoming O-360-A1
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:near Warwick Municipal Airport (N72), NY -   United States of America
Phase: Take off
Nature:Private
Departure airport:Warwick, NY (N72)
Destination airport:Warwick, NY
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On the day of the accident, the pilot decided to take his airplane on a flight around the traffic pattern at his home airport to practice a few takeoffs and landings. After pulling the airplane out of the hangar where he kept it, he performed a preflight inspection. He then performed an engine runup, then back taxied on the runway for takeoff. Once he was in position for takeoff, he advanced the throttle until it was full open, and at 65 mph and about 2/3rds of the way down the runway, he rotated. He immediately realized that the engine was not producing full power, and attempted to advance the throttle further, but he realized that the throttle seemed as though it was not advancing completely. He then nosed the airplane down to attempt to stay in ground effect and gain some airspeed. A lake was at the departure end of the runway, and he was already approaching the trees on the opposite bank. He then picked a spot between trees, turned the fuel off, and pulled the aircraft into a full stall prior to impact.
Postaccident examination of the airplane revealed that the fuselage and wings were substantially damaged. Further examination also revealed that the throttle cable would resist efforts to fully open the throttle and would only move the throttle arm on the carburetor about 1/2 an inch, and when the throttle was fully open, the entire throttle cable would move through the firewall and bulge. After disconnecting the cable from the carburetor, the cable was found to be still under load, until a loose stand-off clamp that connected the throttle cable to the firewall was repositioned, which then allowed the throttle to function properly through its full range of motion.

Probable Cause: A loose stand-off clamp which resulted in a throttle assembly malfunction, and the inability of the engine to produce full power during the attempted takeoff.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA21LA199
Status: Investigation completed
Duration: 4 months
Download report: Final report

Sources:

NTSB ERA21LA199
https://flightaware.com/live/flight/N6448U


Location

Revision history:

Date/timeContributorUpdates
28-Apr-2021 21:50 Captain Adam Added
28-Apr-2021 22:07 Geno Updated [Source]
19-Jul-2021 14:05 aaronwk Updated [Date, Time]
06-Jul-2022 06:42 ASN Update Bot Updated [Time, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

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