ASN Wikibase Occurrence # 25710
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Date: | Saturday 3 August 1996 |
Time: | 07:40 LT |
Type: | Cessna 404 Titan |
Owner/operator: | Superior Aviation, Inc. |
Registration: | N8919G |
MSN: | 4040098 |
Year of manufacture: | 1977 |
Total airframe hrs: | 10624 hours |
Engine model: | CONTINENTAL GTSIO-520-M |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Benton Harbor, MI -
United States of America
|
Phase: | Unknown |
Nature: | Unknown |
Departure airport: | Kalamazoo, MI (KAZO) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot said that during the landing approach, the flight visibility was inadequate for landing, and he aborted the landing. Witnesses observed the airplane touch down long and fast, then it entered fog that shrouded the runway. Subsequently, the airplane collided with trees, then impacted on marshland about 70 feet below the runway elevation. No mechanical anomalies were found with the airplane or engines that would prevent flight. On the day before the accident, the pilot's duty day began at 0500. He had a 9-hour rest period (during the day) that did not involve any sleep. The pilot said that after work on the day before the accident, he arrived home about 2300. His wife said he awoke about 0230 on the accident date, then he returned to bed and arose between 0430 and 0500, departing for work about 0530. During his regular duty day rest period, the pilot would drive a total of 4 hours to and from his home each day. The pilot said he would generally get to bed about 2300 to 2330, arising about 0430 each work day. Also, he said he needed between 6 and 8 hours of sleep at night.
Probable Cause: the pilot's delay in initiating a go-around after not attaining the proper touchdown point during the landing, and his failure to remain clear of obstructions (trees) during the go-around. Factors relating to the accident were the adverse weather condition (fog and low ceiling), pilot fatigue, and the proximity of trees to the runway.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI96LA266 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB CHI96LA266
Location
Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
04-Jan-2011 16:22 |
TB |
Updated [Time, Cn, Phase, Departure airport, Destination airport, Source, Damage, Narrative] |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
15-Sep-2023 07:52 |
Ron Averes |
Updated [[Time, Damage, Category, Investigating agency]] |
09-Apr-2024 05:10 |
ASN Update Bot |
Updated [Time, Cn, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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