ASN Wikibase Occurrence # 267715
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Date: | Tuesday 14 September 2021 |
Time: | 08:40 LT |
Type: | Zenith CH 750 Cruzer |
Owner/operator: | |
Registration: | N161AR |
MSN: | C75-10543 |
Year of manufacture: | 2018 |
Total airframe hrs: | 45 hours |
Engine model: | Viking 130 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Massey Ranch Airpark (X50), Edgewater, FL -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | New Smyrna, FL |
Destination airport: | Greenvillle , TN (4TN5) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot had just purchased the experimental amateur-built airplane and performed a preflight inspection that revealed no anomalies. After departure, the elevator control became momentarily jammed in the nose-down position multiple times, and the pilot elected to return to the departure airport. After two go-around maneuvers due to elevator jamming, the elevator jammed again about 10 ft above the ground during the third landing attempt. The left wing impacted the ground and the airplane veered off the runway and came to rest inverted in a pond.
Postaccident examination of the airframe revealed that the elevator bracket was becoming lodged against a nylon stop block installed in the empennage. It is likely that, while in flight, once the elevator was moved far enough in the nose-down position, the airflow around the elevator forced the elevator to contact the nylon block and jam it in the nose-down position. Examination also revealed evidence of long-term control cable contact with the empennage structure and a lack of tension on the elevator and flight control cables. A mechanic completed a condition inspection, which included examination of the flight control cables and structure, the day before the accident. Based on all available information, it is likely that this inspection was inadequate because it failed to identify and correct the flight control anomalies that ultimately resulted in the accident.
Probable Cause: The mechanic's inadequate inspection of the flight control system, which resulted in a loss of airplane control.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA21LA360 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
|
Sources:
NTSB ERA21LA360
FAA register:
https://registry.faa.gov/aircraftinquiry/Search/NNumberResult?NNumberTxt=161AR Location
Revision history:
Date/time | Contributor | Updates |
14-Sep-2021 16:56 |
gerard57 |
Added |
14-Sep-2021 17:29 |
harro |
Updated [Aircraft type, Registration, Cn, Source] |
14-Sep-2021 17:31 |
harro |
Updated [Location, Phase] |
14-Sep-2021 17:35 |
RobertMB |
Updated [Time, Location, Phase, Destination airport, Source, Narrative] |
14-Sep-2021 17:36 |
RobertMB |
Updated [Narrative] |
14-Sep-2021 17:36 |
RobertMB |
Updated [Phase] |
15-Sep-2021 07:10 |
harro |
Updated [Embed code] |
28-Jul-2023 19:16 |
ASN Update Bot |
Updated [[Embed code]] |
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