ASN Wikibase Occurrence # 35752
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Date: | Tuesday 13 December 1988 |
Time: | 08:54 |
Type: | Rutan VariEze |
Owner/operator: | private |
Registration: | N226RB |
MSN: | 2120 |
Total airframe hrs: | 1627 hours |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Palo Alto, CA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Swansboro, CA |
Destination airport: | Palo Alto, CA (PAO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE ACFT CRASHED 200 FT SHORT OF THE RWY IN A POND AND NOSED OVER. WITNESSES HEARD THE SOUNDS OF LOW POWER. EVIDENCE OF LOW/NO POWER WAS SHOWN BY THE PROP. INVESTIGATION REVEALED THAT UNAPPROVED ENGINE MODS WERE MADE BY PILOT/OWNER. AN UNTESTED CARB HEAT SYSTEM WAS INSTALLED. THE CONTROL CABLE SYSTEM WAS NOT PROPERLY MOUNTED IN THE COCKPIT; IT WAS LOOSE NEAR THE CONTROL STICK WITH NO VISIBLE MEANS OF BEING HELD IN THE CARB HEAT ON POSITION. ADDITIONALLY, THE CARB HEAT AIR DUCT, MOUNTED IN CLOSE PROXIMITY TO THE NO.4 EXHAUST PIPE, HAD NO PROVISIONS ON THE INLET OF THE DUCT TO CONCENTRATE HEATED AIR FOR PREVENTION OF CARBURETOR ICE. CONDITIONS CONDUCIVE TO CARBURETOR ICING EXISTED. CAUSE:
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001213X27433 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:22 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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