ASN Wikibase Occurrence # 38144
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Date: | Thursday 26 February 1998 |
Time: | 07:50 |
Type: | Lancair IV |
Owner/operator: | Private |
Registration: | N109GF |
MSN: | LIV-109 |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Garwood, ID -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Coeur D' Alene Air Terminal, ID (COE) |
Destination airport: | Billings-Logan International Airport, MT (BIL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On February 26, 1998, approximately 0750 Pacific standard time, an experimental Freije Lancair IV, N109GF, impacted a personal residence about three miles southeast of Garwood, Idaho. The commercial pilot and his passenger, who possessed a private pilot's license, received fatal injuries. The aircraft, which was built, owned, and operated by the commercial pilot, was destroyed. The 14 CFR Part 91 personal pleasure flight, which departed Coeur D' Alene Air Terminal about five minutes prior to the crash, had been on an IFR departure in instrument meteorological conditions (IMC). His IFR flight plan was from Coeur D'Alene to Billings, Montana. There was no report of an ELT transmission.
The pilot of the experimental aircraft, who had been on an IFR departure in instrument meteorological conditions (IMC), began maneuvering around the vicinity of Alpine Lake. After a period of between three to five minutes, the pilot lost control of the aircraft, descended out of the low ceiling, and impacted an unoccupied personal residence. At the time of the accident, it was snowing heavily in areas around Alpine Lake, and the visibility was estimated to be one-half mile or less. After the accident, a review of the pilot's log showed that he had recorded only one and nine-tenths hour of instrument time in the last year, and only one hour in the last six months. His log did not show any hours of actual or simulated instrument time in the model aircraft he was flying at the time of the accident. There was no evidence of any pre-impact engine anomaly or vacuum system malfunction.
Probable Cause: The pilot's failure to maintain aircraft control after entering known adverse weather. Related factors were, the pilot's failure to follow the published IFR departure procedures, low ceilings and snow, and the pilot's lack of recent instrument experience.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001211X09609 Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
18-Oct-2022 11:39 |
Captain Adam |
Updated [Operator, Departure airport, Destination airport, Narrative, Accident report, Photo] |
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