ASN Wikibase Occurrence # 42906
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 20 January 1993 |
Time: | 18:05 |
Type: | Beechcraft A35 Bonanza |
Owner/operator: | Rent And Lease Programs |
Registration: | N595B |
MSN: | D-1616 |
Total airframe hrs: | 4950 hours |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Tulare, CA -
United States of America
|
Phase: | Take off |
Nature: | Training |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE CFI IN THE RIGHT SEAT WAS GIVING DUAL TO THE LEFT SEAT CFI, WHO HAD NO EXPERIENCE IN TYPE. DURING THE INITIAL CLIMB, AT ABOUT 400-500 FT AGL, WITNESSES HEARD THE ENGINE LOSE POWER OR SURGE. THE AIRPLANE WAS SEEN TO ROLL TO ONE SIDE AND DESCEND STEEPLY TO IMPACT. THE AIRPLANE HAD BEEN EXTENSIVELY MODIFIED WITH AN UNAPPROVED WING TIP FUEL TANK SYSTEM ADDITION. THE FUEL SELECTOR VALVE FOR THE TIP TANKS DID NOT HAVE ANY PLACARDS SHOWING POSITION OR OPERATION. BOTH CFI'S HAD BEEN GIVEN INCORRECT INSTRUCTIONS ON HOW TO POSITION THE FUEL SYSTEM SELECTOR VALVES BY THE OWNER AND A MECHANIC WHO SIGNED OFF THE ANNUAL INSPECTION. POST-CRASH EXAMINATION REVEALED THAT THE STANDARD FACTORY FUEL SELECTOR WAS IN THE AUX POSITION, AND THE TIP TANKS FUEL SELECTOR VALVE WAS IN A HALF-ON/HALF-OFF POSITION. THE AIRPLANE ALSO HAD A POWERPLANT MODIFICATION FOR INCREASED HORSEPOWER AND OTHER AIRFRAME MODIFICATIONS, NOT ALL OF WHICH WERE DOCUMENTED OR APPROVED. THIS WAS THE FIRST FLIGHT SINCE THE ANNUAL INSPECTION. CAUSE: THE INSTALLATION OF AN UNAPPROVED WING TIP FUEL TANK SYSTEM; AN INADEQUATE ANNUAL INSPECTION WHICH DID NOT NOTE, OR CORRECT, THE UNAPPROVED FUEL SYSTEM ADDITION; A WING TANK FUEL SELECTOR VALVE INSTALLATION WITHOUT ADEQUATE PLACARDS TO SHOW POSITION OR OPERATION; AND INCORRECT INSTRUCTIONS TO THE PILOTS BY THE OWNER AND MECHANIC ON POSITIONING FUEL SELECTOR VALVES WHICH LED TO INADVERTENT MISPOSITIONING BY THE PILOTS AND SUBSEQUENT FUEL STARVATION. IN ADDITION, THE PILOT AT THE CONTROLS FAILED TO MAINTAIN ADEQUATE AIRSPEED FOLLOWING THE POWER LOSS WHICH RESULTED IN AN INADVERTENT STALL/SPIN. A FACTOR WHICH CONTRIBUTED TO THE LOSS OF CONTROL WAS THE DARK NIGHT LIGHT CONDITION.
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001211X11709 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation