ASN Wikibase Occurrence # 43893
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Date: | Tuesday 2 January 2007 |
Time: | 14:00 |
Type: | Beechcraft 58 Baron |
Owner/operator: | Private |
Registration: | N678DC |
MSN: | TH-1517 |
Year of manufacture: | 1987 |
Total airframe hrs: | 2438 hours |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Washington, IN -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Washington, IN (DCY) |
Destination airport: | Hartford, KY (7K4) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane impacted trees and terrain while attempting to return to the departure airport after takeoff. The pilot of another airplane who witnessed the takeoff reported that the accident airplane's takeoff appeared "normal." After takeoff, he noticed the accident airplane about 1.5 miles from the departure airport. It appeared to be in a 45 to 60-degree bank turn back towards the airport, below the level of a tree line. The accident airplane subsequently struck the tree line and came to rest in an agricultural field. The post accident inspection did not reveal any anomalies associated with a pre-impact failure of the flight control system. In addition, examination of both engines did not reveal any failures or malfunctions consistent with a loss of engine power prior to the accident. Examination of the left alternator indicated that it was unable to provide the rated electrical power. Examination of the right alternator did not reveal any anomalies, and the unit appeared to be functional. According to an acquaintance of the pilot, the accident airplane was en route to a maintenance facility for a routine annual inspection. He noted that the left alternator appeared to be inoperative prior to the accident flight and that the mechanic had been advised to look at it during the inspection. He knew of no other problems with the airplane prior to the accident flight.
Probable Cause: The pilot's failure to maintain clearance from trees and terrain while attempting to return to the departure airport for undetermined reasons after takeoff. The intervening tree line was a contributing factor.
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070110X00035&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
04-Dec-2017 18:27 |
ASN Update Bot |
Updated [Operator, Other fatalities, Source, Narrative] |
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