ASN Wikibase Occurrence # 44677
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Date: | Monday 11 October 2004 |
Time: | 17:48 |
Type: | Piper PA-28-161 Warrior |
Owner/operator: | Danbury Flight School |
Registration: | N233PA |
MSN: | 28-7816676 |
Year of manufacture: | 1978 |
Total airframe hrs: | 11703 hours |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Madison, CT -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Nantucket Memorial Airport, MA (ACK/KACK) |
Destination airport: | Danbury Airport, CT (DXR/KDXR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On October 11, 2004, about 1748 eastern daylight time, a Piper PA-28-161, N233PA, was substantially damaged when it impacted a private residence in Madison, Connecticut, while attempting to execute a forced landing. The certificated private pilot and passenger were fatally injured. Visual meteorological conditions prevailed for the personal flight that departed Nantucket Memorial Airport (ACK), Nantucket, Massachusetts, destined for Danbury Municipal Airport (DXR), Danbury, Connecticut. No flight plan was filed for the flight, which was conducted under 14 CFR Part 91.
The pilot made a "Mayday" call, and reported that he was at 4,000 feet msl and descending without engine power. An approach controller acknowledged the pilot's distress call, and attempted to direct him to a nearby airport. The pilot subsequently elected to perform a forced landing to a field; however, during the landing the airplane impacted a private residence. A witness, located about 4 miles north of the accident site, saw the accident airplane flying normally, then heard a "bang." He then heard about 5 seconds of intermittent engine noise, followed by white smoke, which began trailing behind the airplane as it flew. The propeller was found about 3.4 miles from where the airplane came to rest. Examination of the airframe revealed no mechanical anomalies, and examination of the engine revealed damage consistent with an engine overspeed. Examination of the propeller, propeller flange, and associated hardware revealed signatures consistent with insufficient propeller retention bolt torque.
Probable Cause: A loss of engine power due to separation of the propeller due to under-torqued retention bolts.
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20041025X01689&key=1 Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Location
Images:

Photos: NTSB
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Dec-2017 18:28 |
ASN Update Bot |
Updated [Departure airport, Destination airport, Source, Narrative] |
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