ASN Wikibase Occurrence # 87266
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Date: | Monday 3 January 2011 |
Time: | 18:52 |
Type: | Cessna 172H |
Owner/operator: | Private |
Registration: | N1416F |
MSN: | 17254911 |
Year of manufacture: | 1966 |
Total airframe hrs: | 2134 hours |
Engine model: | Continental 0-300 SER |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Walnut Grove -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Ft Leonard Wood, MO (TBN) |
Destination airport: | Bartlesville, OK (BVO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The accident occurred during the fourth leg of a visual flight rules cross-country flight. The pilot departed on the first leg of the trip shortly after sunrise, about 11 hours prior to the accident. The pilot made 3 intermediate stops during the day, where he purchased fuel. The accident flight was approximately 1 hour in duration and was conducted in night visual meteorological conditions. Radar track data depicted the airplane established on a west-southwest course and at a constant altitude. About 15 seconds prior to the accident, the airplane entered a descending left turn, and spiraled down, ultimately impacting an open field. A postaccident examination of the airplane did not reveal any anomalies consistent with a preimpact failure or malfunction. Postmortem toxicology testing was consistent with the prior use of a prescription anti-anxiety medication and marijuana. Due to limited samples, a determination could not be made as to when the substances were last used. Accordingly, no determination was made as to whether the pilot was impaired at the time of the accident. While the departure from controlled flight suggested spatial disorientation, and the extended duration of the trip likely contributed to pilot fatigue, the exact nature of the loss of control could not be determined.
Probable Cause: The pilot's loss of control for undetermined reasons. Contributing to the accident was the pilot's fatigue.
Sources:
NTSB
FAA register:
http://www.ozarksfirst.com/fulltext?nxd_id=380416 http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=1416F Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN11LA138 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Location
Revision history:
Date/time | Contributor | Updates |
05-Jan-2011 08:40 |
gerard57 |
Added |
05-Jan-2011 08:41 |
harro |
Updated [Aircraft type, Registration, Cn, Operator, Source, Damage] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 18:47 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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